A lot of good information here. AC, NOW you know why I said it was a nightmare. Congrats on getting the job done so quickly, I think I was down over a week the first time for the check and adjustment. I think I could do it way faster now that I know what to do and I have learned a few tricks. Your experience make makes 5 of us now that have needed adjustment on the first check. Personally I will NEVER skip a check.
The electronics tray does not need to come all the way out but nearly so. Mainly you have to get the top loose enough that you can pull the main wire harness out through the right side of the frame and out of the way. Truly a royal PIA but worth it when you go to put the cover back on.
Tip on removing the tray: The biggest headache is getting the one bolt that comes in from the back. You can see the threaded tip from the outside, it is in plain view and easy to get to, but the head is on the back side and in a recess that there is no way to see. You have to reach and feel to find it. Really fun to get out and even more "fun" to get back in. You have to use the long part of an allen wrench to reach and you can only turn about 1/4 turn at a time due to limited space. So when I had the bolt out, I cut a small slot in the tip. After that it was way easier because I could put a small screwdriver through the hole and turn the bolt from the outside. To get it started, I pushed the bolt into place with my right hand and turned it from the outside with the screwdriver with my left. Easy. You still have to use a 5MM allen wrench to tighten it but only the last little bit. It is now about 10 times faster to get in and out and a lot less cuss words.
As to the tensioner plunger, yes it really a pain. You have to push it in and turn it at the same time and there is something like 50 to 70 LB of force from the spring and it has oil on it. ???
You are a REAL man if you can do that with our bare hands! ::008::
Here is how I did it. I put it in the vice. The trick was to experiment with the vice padding to get the correct friction on each end. You need the side with the tensioner body to slip enough to allow you to turn it but the piston has to not slip. That way I could slowly squeeze it in the vice as I turned the body to screw it in. It took a bit experimenting but I think I ended up with rubber from an old tube on the piston (no slip) side, and oiled leather on the body (slip) side. After that is was relatively easy. And yes the new one came retracted. ::008::